dom 2.0 ralliart dyno results inside
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dom 2.0 ralliart dyno results inside
Ok so here are the results to my tuning at Modified by KC. Mods on the car are Dom 2.0 turbo, complete evo x swap, 3" TBE, DW 800cc injectors, GrimmSpeed 3 port EBCS, Boost pill removed, K&N Cone filter. It was about 94 degrees on 91 octane. What do you guys think?
Last edited by hixlancer; Aug 9, 2011 at 09:00 PM.
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Just the opposite, a 3-port will maintain better boost stability than the pill.
Looks like there is a struggle with the boost from 5500 on ward. There is a known dip at 5500, but it shouldn't last more than a couple hundred RPM's. It seems to carry all the way to 7000?? Maybe take a look at the WGDC and/or error correction?
EDIT: actually it could be a lot of things. what is the psi on the actuator? If its really low then even giving it 100% WGDC don't do much to help that drop off. I don't know a whole lot about the DOM's, but it looks to be having issues breathing from 5500-7000?
Looks like there is a struggle with the boost from 5500 on ward. There is a known dip at 5500, but it shouldn't last more than a couple hundred RPM's. It seems to carry all the way to 7000?? Maybe take a look at the WGDC and/or error correction?
EDIT: actually it could be a lot of things. what is the psi on the actuator? If its really low then even giving it 100% WGDC don't do much to help that drop off. I don't know a whole lot about the DOM's, but it looks to be having issues breathing from 5500-7000?
Last edited by sstevojr; Aug 10, 2011 at 12:09 PM.