Stock turbo.. Ivey tune
this is stock downpipe??
whats up with all the smoke???? youhave a cat. that should catch 99% of the crap that would come out... looks like she is smoking alot.????? looks like fuel to me. 330 is very nice... but not for a 9 with the mods you have...should be a little higher.
whats up with all the smoke???? youhave a cat. that should catch 99% of the crap that would come out... looks like she is smoking alot.????? looks like fuel to me. 330 is very nice... but not for a 9 with the mods you have...should be a little higher.
Yes stock downpipe and hfc... I'm ordering the downpipe, intercooler piping, cams sometime this month... The afr I have no clue the dyno sheet I put up is the only info i got from the tune. as far as the clutch it's still stock but not for long
Nice #'s i'm at the same power level (330hp/323tq) @ 23psi. I have a AMS tbe w/HFC, licp, gsc S2's, valve springs and adjustable cam gears otherwise are mods are the same. Tuned at ams by Chris, 11.4:1 a/f ratio. I'll get around to posting up a dyno sheet, and a idle video one of these days.
What kind of cams are you going with??
What kind of cams are you going with??
I Just got my Evo 9 tuned and I was dissapointed in the numbers. dyno dynamics dynamometer. 22psi, whp was 281.6 and torque 298. seems a little low. I have a injen intake, nisei fmic. uicp and lower incp, perrin high flow cat. perrin downpipe. hks ti carbon exhaust. Hallman mbc, and deatschwerks 750cc injectors, walboro 255lph. when they were done tuning I started my car to leave and it was knocking. found out they injectors they just installed 2 of them were loose. could this have effected the tuning thus less horsepower? my cousin has the same exact set up minus the injectors, tuned at the same place and has 337 whp and 365 torque. any suggestiions? boost leak?
its just as hard on the clutch my opinion though mine stock clutch held 389 tq for about a week only launched once and ran up 2 mountains with a new gtr and zo6 hung well with them
I Just got my Evo 9 tuned and I was dissapointed in the numbers. dyno dynamics dynamometer. 22psi, whp was 281.6 and torque 298. seems a little low. I have a injen intake, nisei fmic. uicp and lower incp, perrin high flow cat. perrin downpipe. hks ti carbon exhaust. Hallman mbc, and deatschwerks 750cc injectors, walboro 255lph. when they were done tuning I started my car to leave and it was knocking. found out they injectors they just installed 2 of them were loose. could this have effected the tuning thus less horsepower? my cousin has the same exact set up minus the injectors, tuned at the same place and has 337 whp and 365 torque. any suggestiions? boost leak?
was your injector leaking like could you smell gas ? to be honest they should have had test for a boost leak and also logged the boost , if its knocking like your car is bucking it could be a boost leak i have had that problem thought i was the tune cause i couldn't watch the boost it was so bad


