Notices
Evo Dyno Tuning / Results Discuss vendor and member dyno tuning techniques, results and graphs.

LR 2.4 HTA 3586 on E85

Thread Tools
 
Search this Thread
 
Old May 19, 2011, 01:52 PM
  #31  
Evolving Member
iTrader: (22)
 
ta ace's Avatar
 
Join Date: Jun 2010
Location: wichita, KS
Posts: 411
Likes: 0
Received 0 Likes on 0 Posts
Originally Posted by tscompusa
me. we will baseline it also on the current tune that way theres something to compare to with gains. it will probably take awhile tho before the results are posted.. the sd needs lots of work for drivability.
Told him to go to you tom lol my car drives as if stock and pulls like a race car. lol
Old May 19, 2011, 02:53 PM
  #32  
Former Sponsor
iTrader: (22)
 
tscompusa2's Avatar
 
Join Date: Oct 2005
Location: pa
Posts: 5,375
Likes: 0
Received 7 Likes on 7 Posts
Originally Posted by ta ace
Told him to go to you tom lol my car drives as if stock and pulls like a race car. lol
ya i know i shipped him a programmer before you referred me to him though. thanks for the referral.
Old May 19, 2011, 03:41 PM
  #33  
Evolved Member
Thread Starter
iTrader: (24)
 
localtoys73's Avatar
 
Join Date: Oct 2008
Location: deltona
Posts: 1,028
Likes: 0
Received 1 Like on 1 Post
I will just be glad to be near the end of this long journey. I hope to make some good power and have the car as close to stock as possible.
Old May 31, 2011, 04:46 PM
  #34  
Evolved Member
Thread Starter
iTrader: (24)
 
localtoys73's Avatar
 
Join Date: Oct 2008
Location: deltona
Posts: 1,028
Likes: 0
Received 1 Like on 1 Post
stupid car is stupid.
tune was going great making awesome power then has a 34 to 46lbs boost spike and popped the head gasket.

Just ordered new gasket from MAP with there head studs.
Going to swap out to a manual boost controller and go back at it later this month.
Made well over 700hp before the damage.
Old May 31, 2011, 04:48 PM
  #35  
Former Sponsor
iTrader: (22)
 
tscompusa2's Avatar
 
Join Date: Oct 2005
Location: pa
Posts: 5,375
Likes: 0
Received 7 Likes on 7 Posts
Originally Posted by localtoys73
stupid car is stupid.
tune was going great making awesome power then has a 34 to 46lbs boost spike and popped the head gasket.

Just ordered new gasket from MAP with there head studs.
Going to swap out to a manual boost controller and go back at it later this month.
Made well over 700hp before the damage.
should have waited till i got unbusy to tune it.. boost doesnt just spike from 34 to 46 .. something was clearly done wrong. boost error correction tables are your friend.
Old May 31, 2011, 05:00 PM
  #36  
Evolved Member
Thread Starter
iTrader: (24)
 
localtoys73's Avatar
 
Join Date: Oct 2008
Location: deltona
Posts: 1,028
Likes: 0
Received 1 Like on 1 Post
went with diirk from awd becaue he is pretty local to me. He was going up 4% each time every thing was going smooth until we got to 34lbs then we hit the spike. I am not sure what caused it my only idea is the controller. Possibly the wastegate although I dont see how.
Old May 31, 2011, 05:11 PM
  #37  
Evolved Member
iTrader: (15)
 
FL_SilverEvo8's Avatar
 
Join Date: Oct 2005
Location: Fort Myers, FL
Posts: 1,139
Received 0 Likes on 0 Posts
What controller are you using?
Old May 31, 2011, 05:14 PM
  #38  
EvoM Guru
iTrader: (1)
 
RSMike's Avatar
 
Join Date: Jul 2009
Location: New Zealand
Posts: 2,225
Received 304 Likes on 122 Posts
Originally Posted by localtoys73
went with diirk from awd becaue he is pretty local to me. He was going up 4% each time every thing was going smooth until we got to 34lbs then we hit the spike. I am not sure what caused it my only idea is the controller. Possibly the wastegate although I dont see how.
he didn't back off when it spiked that high?
Old May 31, 2011, 05:15 PM
  #39  
Evolved Member
Thread Starter
iTrader: (24)
 
localtoys73's Avatar
 
Join Date: Oct 2008
Location: deltona
Posts: 1,028
Likes: 0
Received 1 Like on 1 Post
he did but the spike was quick he let off right when it happened. power went from 675 to almost 800 at that moment.

by then the damage was done. Car still runs I just cant boost over 35 or it leaks.
Old May 31, 2011, 05:19 PM
  #40  
Former Sponsor
iTrader: (22)
 
tscompusa2's Avatar
 
Join Date: Oct 2005
Location: pa
Posts: 5,375
Likes: 0
Received 7 Likes on 7 Posts
Originally Posted by localtoys73
went with diirk from awd becaue he is pretty local to me. He was going up 4% each time every thing was going smooth until we got to 34lbs then we hit the spike. I am not sure what caused it my only idea is the controller. Possibly the wastegate although I dont see how.
spike or creep? was it ran on a different gear in that run? are the boost error correction tables all set to 0? (not recommended for the final tune)

sounds like the line came off the wastegate or something of that nature. no problem i understand going to a dyno anyways.. its a little dangerous road tuning 700whp+ on the street. sounds like its turning into a beast tho
Old May 31, 2011, 05:27 PM
  #41  
Evolved Member
Thread Starter
iTrader: (24)
 
localtoys73's Avatar
 
Join Date: Oct 2008
Location: deltona
Posts: 1,028
Likes: 0
Received 1 Like on 1 Post
was using a ebc(not sure the brand) will switch to mbc( I think that is culprit) no lines came off we checked

it was a spike not creep I will post graphs once I get them sent to me. It was crazy thats for sure.
Car runs allot smoother then before with allot less timing which is always a good thing.

Yes 600 on the streets is crazy 700 or 800 is insane.

I know the car will make good power though just have to figure out the small stuff I guess.
Old May 31, 2011, 05:46 PM
  #42  
Former Sponsor
iTrader: (22)
 
tscompusa2's Avatar
 
Join Date: Oct 2005
Location: pa
Posts: 5,375
Likes: 0
Received 7 Likes on 7 Posts
so from what i gather the head only lifts at 35psi? have you removed the valve cover and checked the torque specs on the headstuds? maybe they just need retorqued.....?
Old May 31, 2011, 05:52 PM
  #43  
Evolved Member
iTrader: (6)
 
mt057's Avatar
 
Join Date: Apr 2007
Location: DFW
Posts: 1,529
Received 12 Likes on 11 Posts
Originally Posted by localtoys73
went with diirk from awd becaue he is pretty local to me. He was going up 4% each time every thing was going smooth until we got to 34lbs then we hit the spike. I am not sure what caused it my only idea is the controller. Possibly the wastegate although I dont see how.
I recently had a fray in my signal wire which caused my system to spike. Everything would be fine until about 6000 Rpm then bam straight to the moon. I believe that the frayed wire was giving improper voltage so once it was supposed to reach full current it would freak out because it was not.
Old May 31, 2011, 06:01 PM
  #44  
Evolved Member
iTrader: (6)
 
bambooi's Avatar
 
Join Date: Sep 2005
Location: NC
Posts: 527
Likes: 0
Received 0 Likes on 0 Posts
Could slowly increasing the fuel cut load prevent the problem?
Old May 31, 2011, 06:06 PM
  #45  
Evolved Member
Thread Starter
iTrader: (24)
 
localtoys73's Avatar
 
Join Date: Oct 2008
Location: deltona
Posts: 1,028
Likes: 0
Received 1 Like on 1 Post
Originally Posted by tscompusa
so from what i gather the head only lifts at 35psi? have you removed the valve cover and checked the torque specs on the headstuds? maybe they just need retorqued.....?
After the spike we started back at 28lbs and went up slowly we made it to 34lbs and then it spiked again to 39lbs (it leaked again at the spike). going to take it apart next week so not sure what the damage is. We will try to retorque first. It held fine at the 28, 30, and 32lbs pull.

Wont know much until we take it apart.


Quick Reply: LR 2.4 HTA 3586 on E85



All times are GMT -7. The time now is 01:25 PM.