The Big Turbo "still running" Motor club (Evo X only, please)
#16
Evolving Member
Thread Starter
Nice man! What are the tq numbers looking like?
#19
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Join Date: Feb 2007
Location: Las Vegas, NV
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Count me in...
-2010 GSR
-14,500 miles
-mods listed in the sig
-FP Black (Journal)
-425/355 @ 24 psi on a dynojet
-Roughly 3,000 miles on the turbo. Not my daily driver
-Spirited driving. Hasn't made it to the track... Yet. Suspension work in the next few weeks. Maybe a track day or two this summer.
-Staying conservative until the build.. Maybe this winter
-2010 GSR
-14,500 miles
-mods listed in the sig
-FP Black (Journal)
-425/355 @ 24 psi on a dynojet
-Roughly 3,000 miles on the turbo. Not my daily driver
-Spirited driving. Hasn't made it to the track... Yet. Suspension work in the next few weeks. Maybe a track day or two this summer.
-Staying conservative until the build.. Maybe this winter
#22
Evolving Member
Thread Starter
Count me in...
-2010 GSR
-14,500 miles
-mods listed in the sig
-FP Black (Journal)
-425/355 @ 24 psi on a dynojet
-Roughly 3,000 miles on the turbo. Not my daily driver
-Spirited driving. Hasn't made it to the track... Yet. Suspension work in the next few weeks. Maybe a track day or two this summer.
-Staying conservative until the build.. Maybe this winter
-2010 GSR
-14,500 miles
-mods listed in the sig
-FP Black (Journal)
-425/355 @ 24 psi on a dynojet
-Roughly 3,000 miles on the turbo. Not my daily driver
-Spirited driving. Hasn't made it to the track... Yet. Suspension work in the next few weeks. Maybe a track day or two this summer.
-Staying conservative until the build.. Maybe this winter
#24
Evolving Member
Thread Starter
#26
Evolving Member
Thread Starter
#28
Evolving Member
Thread Starter
So here's what happened... I went to get tuned yesterday and Ivey said my boost was dropping on its face for some reason and couldn't get more than 370WHP... so I had to do a pressure test that revealed the gasket between the turbo and the uicp was leaking (I believe it's a one time use) Ivey then put it back on the dyno and got 415whp out of it. He said the boost was jumping around and told me to come back today and get the wastegate adjusted. He then street tuned the car and said it was feeling better. The car feels nice and strong, I'd suspect at least 420 if it was on the dyno again. But like I told Ivey that number is perfect for now until I build the block.
#30
Evolving Member
Thread Starter