Going lean above 6000
I thought you said you used JohnBradley's values for the latency so my assumption was if his were wrong and JohnBradley tuned his then mine would be also but now I see you aren't using his. My issues aren't tune related, they're hardware, something is going wacky with my car and I'm trying to pin point it to fpr, fuel filter, fuel line, or injectors and possibly map sensor...I used to say I was blessed with a smooth running car, now she's showing her true colors *sigh* I know you're busy tuning so didn't want to bother you with stuff non-tune related. It's some fuel distribution issue. See -
https://www.evolutionm.net/forums/ev...-attached.html
https://www.evolutionm.net/forums/ev...-attached.html
if not that then injector related.
Last edited by tscompusa2; Jul 15, 2011 at 04:58 PM.
I thought you said you used JohnBradley's values for the latency so my assumption was if his were wrong and JohnBradley tuned his then mine would be also but now I see you aren't using his. My issues aren't tune related, they're hardware, something is going wacky with my car and I'm trying to pin point it to fpr, fuel filter, fuel line, or injectors and possibly map sensor...I used to say I was blessed with a smooth running car, now she's showing her true colors *sigh* I know you're busy tuning so didn't want to bother you with stuff non-tune related. It's some fuel distribution issue. See -
https://www.evolutionm.net/forums/ev...-attached.html
https://www.evolutionm.net/forums/ev...-attached.html
ill check the thread out.. im on aim dont be afraid to contact me. just because im busy doesn't mean i wont still talk.
It wasnt the SD settings, it was a math mistake on something else simple. Like I said its sorted and he has a new map to match the mods.
Last edited by JohnBradley; Jul 15, 2011 at 02:04 PM.
injector scaling lol. the extra engine displacement changes confused him probably. right? i dont think he cares if you post what it was. everyone makes mistakes.
I figured out my issue...two almost 100% clogged injectors, 1 was about 60% clogged, one was clear. The two clogged wouldn't even pull fuel through *sigh* They're being overnighted to FIC. UGH, f'in e85 *double sigh* I got lucky, damn e85 showed no knock...keep an eye on that wideband gauge from time to time guys!
Thread Starter
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Not at all but the good news is that it is fixed! Not sure how but it holds 11.5 from 4-8k perfect in 4th, had nearly the whole car apart, battery disconected for two hours, inspected everything and it flys again, I'm happy at this point.
This may sound stupid but did u ever think it maybe the wideband sensor thats bad?same thing was happening to a friend of mine and he did everything..found nothing then changed his sensor n it was the problem.
Glad that your car stopped being a *****, now lets see some numbers from this beast with the black!
This sounds very familiar... still sorting out the issue, but it seems to be improving. Initially seemed like a scaling issue. If I scaled the injector size higher, it would drive better, but the A/F ratios refused to get richer at WOT. If I scaled the size lower, full throttle improved, but at the expense of driveability. Also running FIC 2150s
Dan
Dan
Try scaling the injectors incrementally smaller and report back. That is exactly what I had to do. Also with such a larger injector I was having issues with tip in throttle being too rich, so I dialed back substantially accel enrichment and that improved driveability.
Dan
Dan







, not a ROM issue at all.
