"JUNK BOX" Complete!! 8s???
Took the Junk Box to my office complex for work today! Street Car!
Its about 90 degress here and the car is running great!
Tomorrow it is getting the new Spark Tech Sequential Ignition on the car and alignment Friday! I will be driving the car to the alignment rack on Friday. Stay tuned, here a quick pic of the car at work
Its about 90 degress here and the car is running great!
8 sec Time slip hopefully to come. Ill keep everyone updated on how this weekend goes at the Dyno!

UPDATE!!
Hey everyone,
I know i have been out of the loop the last couple weeks. Been busy with work and trying to get things done. As for the Junk Box. We did a compression check early last week. I brought the car to Devin to get some things tweaked before the Dyno last Saturday. We did the compression check and it read 150/150/80/145. Cylinder 3 has some big time issues. Leaking through the rings and some bad valves in the head.
I was not too happy with the results of the test. Basically came down to fixing peoples mistakes. However, I didnt get upset or discouraged. When my first turbo let go, shavings got in my motor and had knicked the top of the pistons. 3 of the are usable and the other one is not. Since then i bought a new 6765 and through it on there. Went to the Dyno made that power and wenty 9.1. I bought brand new 10:5:1 HD1400 pistons. I went with new bearings, rings, pistons, and newly re-done head by Terry @ Class one. When i made 766WHP on the Stock Ignition the car was down on compression and had some leak down. I went ahead and used the motor to get some track days in. Now with everything being re-done fresh by Devin@Boostin Performace were planning on going on the Dyno this saturday with the new cams!
It was a shock to see the low compression but I knew the head and motor wasnt the healthiest. But im glad im doing this now so upcoming track days and the Shootout I will have a fresh motor and car. Im going to keep everyone updated toward the end of the week and weekend. The following week/weekend I will be going to that track to attempt my 8 second pass
Hey everyone,
I know i have been out of the loop the last couple weeks. Been busy with work and trying to get things done. As for the Junk Box. We did a compression check early last week. I brought the car to Devin to get some things tweaked before the Dyno last Saturday. We did the compression check and it read 150/150/80/145. Cylinder 3 has some big time issues. Leaking through the rings and some bad valves in the head.
I was not too happy with the results of the test. Basically came down to fixing peoples mistakes. However, I didnt get upset or discouraged. When my first turbo let go, shavings got in my motor and had knicked the top of the pistons. 3 of the are usable and the other one is not. Since then i bought a new 6765 and through it on there. Went to the Dyno made that power and wenty 9.1. I bought brand new 10:5:1 HD1400 pistons. I went with new bearings, rings, pistons, and newly re-done head by Terry @ Class one. When i made 766WHP on the Stock Ignition the car was down on compression and had some leak down. I went ahead and used the motor to get some track days in. Now with everything being re-done fresh by Devin@Boostin Performace were planning on going on the Dyno this saturday with the new cams!
It was a shock to see the low compression but I knew the head and motor wasnt the healthiest. But im glad im doing this now so upcoming track days and the Shootout I will have a fresh motor and car. Im going to keep everyone updated toward the end of the week and weekend. The following week/weekend I will be going to that track to attempt my 8 second pass








