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Lancer Aftermarket Forced Induction Tech Discuss forced induction related specs and upgrades for custom aftermarket setups.

05 OZ turbo build

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Old Jul 22, 2011 | 11:44 AM
  #226  
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I haven't been able to stomp it...I got it to get to 107 load and then I had to let off of it. I gotta fix a couple of suspension issues then I should be able to really check. For some reason I don't think its blown though, but I can't back it up but I have that feeling that it is not blown.
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Old Jul 22, 2011 | 12:02 PM
  #227  
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well is there any oil around it?
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Old Jul 22, 2011 | 01:41 PM
  #228  
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not that I could see.
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Old Jul 22, 2011 | 03:46 PM
  #229  
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well if your not smoking out your exhaust either then its probly not blown. there was a couple times i thought mine was too but it wasnt.
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Old Jul 22, 2011 | 06:26 PM
  #230  
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no smoke out the back.
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Old Jul 22, 2011 | 09:09 PM
  #231  
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probly fine. i wonder if there is something internally wrong with my motor causing bad vac at idle and rich closed loop afrs
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Old Jul 23, 2011 | 11:05 PM
  #232  
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ok well here is something weird... i was so frustrated today with my -12 vac that i tried another boost guage but instead just unplugged a hose from the intake mani and plugged it into the boost guage... perfect -20.... weird so then i hook the connection back how it was and replaced the other boost gauge were mine is now... -12 weird... so i thought it was the hose and fooled around with it but it wasnt.

turned out i tried a bunch of different Ts and nothing worked... turns out if i have it not T'ed it works so i stole one off the vacuum control valve... any ideas on this one guys?
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Old Jul 24, 2011 | 04:03 AM
  #233  
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Collapsed vacuum T's??? My gauge is quad point T'd between the fpr and intake with the additional things being bov and vac/boost gauge. Reads- 3hg/inch with the car off....real piece of junk. 4bar omni is dead accurate...that's a killer boost gauge, cause you can log it. And speed density...
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Old Jul 24, 2011 | 11:42 PM
  #234  
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no I tried a bunch of different T's.... how does that make any sense tho?
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Old Jul 25, 2011 | 09:07 AM
  #235  
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How does it make sense that the gauge reads one thing at one nipple but something else at a different nipple? a leak somewhere or a collapsed hose/T....or little engine gremlins blowing in one of the tubes when you're not looking......
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Old Jul 25, 2011 | 09:14 AM
  #236  
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i tried T'ing in at several places on the manifold... but only when i used a T it was messed up. hahaha i dont get it
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Old Jul 25, 2011 | 10:53 AM
  #237  
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Use bigger T's then? are you using little bitty ones?
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Old Jul 25, 2011 | 03:10 PM
  #238  
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well i was using the one the glowshift boost gauge came with and its pretty big. i also tried smaller.
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Old Jul 25, 2011 | 03:57 PM
  #239  
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tried a bigger T and saw 4 vac lol
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Old Jul 25, 2011 | 07:29 PM
  #240  
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On the plus side, you know that as you are making those changes, trying different things, you are seeing results....so you are on the right thing. That's a plus.
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