razorlab's simple build(s)
Evo GSR with SSSL package
Power:
Resonated test pipe
Magnaflow catback with MAP 3" mod
AEM intake
Depo upper IC pipe
GM 3 port boost solenoid
ID1000cc injectors
AGP FMIC
Radium surge tank setup
Walbro 450 E85 pump in surge tank
OEM pump in OEM tank
E75 fuel (E50-E60 last time)
Power:
Resonated test pipe
Magnaflow catback with MAP 3" mod
AEM intake
Depo upper IC pipe
GM 3 port boost solenoid
ID1000cc injectors
AGP FMIC
Radium surge tank setup
Walbro 450 E85 pump in surge tank
OEM pump in OEM tank
E75 fuel (E50-E60 last time)
Thread Starter
Joined: Aug 2003
Posts: 14,094
Likes: 1,092
From: Mid-Hudson, NY
FMIC and Upper IC aren't really power adders either. FMIC is for consistency.
Really? After seeing the way the stock exhaust is built, I was expecting big gain from that upgrade, you're telling me not to waste my money on exhaust other then for a high flow cat?
Regarding the piping, I was expecting boost coming in faster
Thread Starter
Joined: Aug 2003
Posts: 14,094
Likes: 1,092
From: Mid-Hudson, NY
Check out my Ralliart build. I was running stock catback with upgraded turbo and making almost 200whp MORE than stock: https://www.evolutionm.net/forums/09...sportback.html
Thread Starter
Joined: Aug 2003
Posts: 14,094
Likes: 1,092
From: Mid-Hudson, NY
Getting the car ready for another track event coming up next Monday.
Changed all my drivetrain fluids with OEM fluids. I still had factory fill in there with 19k miles and 5 track events. Shame on me.
Fluids actually weren't horrible. The rear diff torque mechanism fluid being the darkest (the clutch bath).
I also wired in my flexconverter ECA. I did this to move my flex sensor out of the engine bay and also to put it on the feed line, to be more **** with flex fuel ECU response.
My fuel tank is becoming a crowded place now!
Changed all my drivetrain fluids with OEM fluids. I still had factory fill in there with 19k miles and 5 track events. Shame on me.
Fluids actually weren't horrible. The rear diff torque mechanism fluid being the darkest (the clutch bath).
I also wired in my flexconverter ECA. I did this to move my flex sensor out of the engine bay and also to put it on the feed line, to be more **** with flex fuel ECU response.
My fuel tank is becoming a crowded place now!
Thread Starter
Joined: Aug 2003
Posts: 14,094
Likes: 1,092
From: Mid-Hudson, NY
Another track event yesterday. It was a day of both joy and sorrow...
The joy was I blew my personal best out of the water and put down a 2:03 lap time, which is only 1 sec off my best I ever did with my Evo 8 at the same track. Super impressed with the Evo 10 now that I have it set up correctly.
I also had an awesome session dueling with a very well setup, driven and powerful VW GTi that impressed me. Had a blast this session:
The sorrow...
The next and last session out the car lost all power coming out of turn one and didn't want to rev. No smoke, no liquid trail behind the car so I limped it into the pits.
Car sounded like it was only running on three cylinders. Pulled the plugs and cylinder number four had a nice present for me....


Put a fresh set of plugs in hoping maybe I got lucky and no luck, still three cylinders only.

So I had a nice 144 mile tow home...

At least the driver was a super cool guy which made the trip seem short.
Logs where clean that session until I hit the rev limiter coming into the front straight and it registered a 17 knock count. Not sure if that was the unlucky moment that the plug decided to peace out but I did WOT all the way down the straight (I didn't notice the knock light because it happened in a high G right turn) to 125mph (and the log was clean) and then the car called it quits powering out of turn one at the end of the straight. Interesting enough the logs where clean except for that 17 count event, so I'm assuming that was the fate and I got unlucky.
I was so beat by the time I got home I just pushed the car into the driveway and went to bed.
Going to do a compression check this weekend and cross my fingers it's just the top end and not the bottom end...
Situation sucks but for doing track events for more than 15 years now and this was the first engine failure, I guess it was just a matter of time, and that time struck yesterday...
The joy was I blew my personal best out of the water and put down a 2:03 lap time, which is only 1 sec off my best I ever did with my Evo 8 at the same track. Super impressed with the Evo 10 now that I have it set up correctly.
I also had an awesome session dueling with a very well setup, driven and powerful VW GTi that impressed me. Had a blast this session:
The sorrow...
The next and last session out the car lost all power coming out of turn one and didn't want to rev. No smoke, no liquid trail behind the car so I limped it into the pits.
Car sounded like it was only running on three cylinders. Pulled the plugs and cylinder number four had a nice present for me....


Put a fresh set of plugs in hoping maybe I got lucky and no luck, still three cylinders only.

So I had a nice 144 mile tow home...

At least the driver was a super cool guy which made the trip seem short.
Logs where clean that session until I hit the rev limiter coming into the front straight and it registered a 17 knock count. Not sure if that was the unlucky moment that the plug decided to peace out but I did WOT all the way down the straight (I didn't notice the knock light because it happened in a high G right turn) to 125mph (and the log was clean) and then the car called it quits powering out of turn one at the end of the straight. Interesting enough the logs where clean except for that 17 count event, so I'm assuming that was the fate and I got unlucky.
I was so beat by the time I got home I just pushed the car into the driveway and went to bed.
Going to do a compression check this weekend and cross my fingers it's just the top end and not the bottom end...
Situation sucks but for doing track events for more than 15 years now and this was the first engine failure, I guess it was just a matter of time, and that time struck yesterday...
Thread Starter
Joined: Aug 2003
Posts: 14,094
Likes: 1,092
From: Mid-Hudson, NY
Factory original. 19k, same as the car. I actually had a fresh set of plugs I was going to change out after the event. Who knows if it was the age or just bad luck. 19k really isn't much on iridiums. The other three looked fine.








